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This is where all of our weekly progress will be recorded

Monday 13/11.23

We started the day by going to St. Olavs and retrieving a styrofoam box and some dry ice.

The rest of the day was spent implementing and testing the cooling method.

This is described on the Cooling page.


We also made a new metal bed by drilling through the holes in our MDF plate, so that the machine will be ready for testing once the cooling method works.


Next we want to repeat the test, but with a full box of dry ice, instead of one that is 1/3 full.



Wednesday 15/11.23 


Today we continued our experiment with a full box of dry ice.

First we turned on the vacuum, sucking air out of the box. What we saw was that our new seal was not air tight enough and air was leaking out through the lid. This reinforces the known issue of trying to vacuum seal something that was not meant to be airtight.


We then went back to the idea of pumping air in through the tube, instead of sucking it in due to vacuum. We used the small 120W hand-pump to pump air through our pipe.


We used an infrared thermometer to measure the temperature of the air going into the box. It was -20*C. The air going out of the handpump, going into the tubing system, was significantly hotter than the environmental air, and even the air going out of our big 1000W vacuum. 


Due to this we decided to create a makeshift heat exchanger by threading an outgoing tube through the ingoing tube of the vacuum. CADs were made at the end of the day and set to print to Thursday.



Thursday 16/11.23 

Today we tested our heat exchanger vacuum adapters. They seem to be looking okay, but some of the dimensions are a bit off. We quickly update the designs and set new prints to be done after lunch. 



I had a productive talk with Henrik Øverbø about our cooling system and the possibilities of optimalization. Short summary:

 - Creating a small closed loop would be more optimal. Longer tubes = less efficient.

 - Read Henriks master, could provide valuable knowledge.



Friday 17/11.23 

Today, we started with a scrum session where Peter, Håvard and Eirik were present

We alse ran some test with the completed heat exchanger setup. We mounted the tube into the vacuum hose and cut the pipes to size.  We have made a cooler spiral from plastic tubes with a wider diameter (Ø9mm) so that more air can be pushed into the freezer. After refilling the isopor box with dry ice, we gave the system some tests.

In the first test we started at 1,9 degrees and the pump pulled it down to -2,3 degrees and stayed there.

In the second test we had let the freezer cool to -4 degrees and is stayed there for 90 sec, and then we turned the vacuum of.
This looks promising. Next will be to cool the freezer further down and see if the system really is able to hold the cold temperatures.

We found some saw-dust in the adapters after testing, so we are considering taking up the search for alternative vacuums.

We also have started ordering organs from Nortura to prepare them for slicing next week.


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