This is where all of our weekly progress will be recorded

Monday 15/01.24

We started the semester with a meeting with Håvard and then a meeting with Martin.

We have outlined a plan for the semester.


We aim to drill a prostate within two weeks. This part of the project is recorded here.


The next step will be improving the sanitation.


Tuesday 16/01.24

Today we have researched ways to implement a filter on the suction, as we believe this will be the most effective way of stopping contamination. 


We went down to the MR Core Labs and discussed with Sebastian what type of filter was standard in cases like this. It is discussed here. He also proposed that we do not spend time disassembling the last prototype, but rather buy new parts for the new prototype as this will both save time, but will also leave us with a functioning prototype that we can use for testing and comparison.

The results from our first day of filter testing was not good. The filter we got to test from Sebastian almost shut down air flow.

Combining this problem with the added complexity the cold removal from the vacuum system, and the still unsolved extraction method, does not bode well for vacuum suction.

Even though these hinderances are slowing the prostate drilling test down, it is a product problem we would've had to meet sometime, so its better to face them now, early on, rather than later.


Tomorrow we will have to keep exploring ways to solve this issue.


Wednesday 17/01.24

We have landed on trying a HEPA filter for our solution. We will need to decide what size we need, we should probably aim for maximum air flow and pressure, and optimize later if needed.


The Vacushield will also have to be tested with a vacuum pump located at MR Core Labs. If the clamping works with that pump and filter combination that would be great. 


We have also started evaluating possible ways to improve the prototype in the coming months.


Thursday 18/01.24

The air flow through the tube connected to the vacuum cleaner was measured to be around 100L/min (v=21m/s, d= 10mm). Based on this number, we decided to order the biggest HEPA-filter available, just to be safe.

In addition, a box made from 6mm acryllic has been made for testing the vacuum pump down at St.Olavs. Work will continue on this tomorrow.


Friday 19/01.24 

The Vacuum tight acryllic box was completed today. Holes were drilled into a baseplate made from 3mm aluminium, which then was mounted to the acryllic box using Tec-7 sealant. Everything was then clamped, and will be left over the weekend to dry. It will hopefully be fully sealed, adn ready to be tested next week


Monday 22/01.24

Peter was sick today, and Øystein had to do some vaccination. Therefore, no work was done today.


Tuesday 23/01.24



Wednesday 24/01.24

Today we decided to split up to increase productivity. Øystein is going to focus on finding a CNC and testing the filters with different pump. Peter will test the popping extraction method and research if there is a freezer we can modify.


We have both began doubting the vacuum gripping solution. We have concluded that the problems it introduces were not as simple as first though.

It does provide an optimal non-invasive gripper and makes it possible to mill several samples on the same procedure, but it bring the requirement of another cooling method, a filter, and a new extraction method. 


We have decided that if the popping extraction works and if we find a filter that works we will have to make an overall assessment on whether we feel it is worth continuing with or not.


The first part of Peters task is complete. Samples are cut in turkey slices and are placed in the freezer to freeze. I had to calibrate the equipment to be sure to not crash into the base plate while milling. The depths i measured was:


Thursday 25/01.24

The vacuum tight acryllic box was tested at St.Olavs today. The vacuum pump there was able to draw around 96 l/min. of air through the box. The ham slices tested were heldt firmly in place when all the holes were covered, even with the filter in place. It lost a lot of effect when half of the holes were left exposed. In conclusion, the vacuum clamping will work, when everything is made to be completely vacuum-tight. In addition, if the "base box" is made from stainless steel, it can be machined to be vacuum tight to a lid via an o-ring. It will also be able to be  sanitized.

We are also allowed to request to borrow the vacuum pump for some days, but this has to be agreed with with Sebastian.


Friday 26/01.24


Today we have continued to research freezers. we found one at elkjøp that is more powerful than the one we found at power. It was difficult to deduct from the images whether or not it has the desired qualities, so we will have to go to the store and inspect it.


We have also tested and evaluated the popping method. It is described here. The conclusion was that it failed.


Monday 29/01.24

We had a little start up meeting with Håvard. Together we came up with an idea of how to make drilling a prostate work. We also laid a plan for testing popping extraction one more time, this time at even colder temperatures and with less temperature fluctuations during milling. This is described in Prostate Extraction under test 2.


Tuesday 30/01.24

The main plan for today is to have a discussion with Sebastian about the way forward, and then execute popping extraction test 2 and begin preparations for popping extraction test 3.

The MR Core Labs team requested a statement regarding the projects progress so far and its state at this time, as well as a rough weekly plan so that they can better plan ahead. This plan can be found here.

We also tested the popping extraction method with the samples being left in the freezer overnight, before being put into a box filled with dry ice, with a temp of around -100*C. The tests resulted in the slice shattering into pieces, with the samples also shattering. Images can be found here Therefore, another slice will be milled, and extraction at a lower temperature will be performed tomorrow.


Wednesday 31/01.24

Today we conducted extraction popping test 3 and got good results. Many samples were extracted without harm to the slice or sample. The best success rate was achieved when we used a scalpel to further weaken the bond between slice and sample. 


With this we now have a complete overview of what benefits and disadvantages comes with vacuum gripping. After consideration we have chosen to pivot from the vacuum gripping solution and instead incorporate a solution more similar to the one currently in use at MR Core Labs, only automatic. Even though the vacuum gripping with popping extraction would be possible to perform, we feel that the concept bring too many extra components and therefore possible complications to the product. In addition we believe that we can guarantee a higher success rate, less workload for the operator, and a less complicated product to learn/operate with normal clamping. 


We will still perform a test tomorrow regarding the effect of spooning on the extraction of the slice.


Going forwards we want to start creating rough designs of how we envision the final product to look/work, as well as incorporating any components necessary for prostate milling into the ARTS 1.0. 


Thursday 01/02.24

Today we performed popping extraction test 4. This is further described here.


We began creating the design for the new gripping solution. This is further described here.


We started making the base-box that we need for the prostate cutting. This is further described here.


Finally we have started making an outline of our thesis.


Friday 02/02.24

The base box for prostate cutting was improved further today. Read about it here.


Monday 05/02.24

We finished the testing the performance of the CNC and it's electronic components after long time exposure to a cold environment. We left the freezer on for around 1 week, at around -18 degrees Celsius. The conclusion from this experiment was that the electronics still functioned as intended after being frozen for 1 week. However, there were some sqealing from the lead screws, which could be solved using a lubricant ment for cold environments.

In addition, we have started planning the milling locations for the prostate. but untill we know how large the prostate slice is, this is going to be put on hold.


Tuesday 06/02.24

Today the freezer arrived and so the design for the final product began. Information about the freezer has been stored here.

The rough plan for the design is something like this:



We also found a viable CNC, that we will be considering tomorrow.


Wednesday 07/02.24

Today we ordered the CNC.

The rest of the day was spent researching other necessary components for the final product.

Øystein looked into cam levers and cameras, while Peter explored the temperature sensor array.


Thursday 08/02.24

This day was used to read through some HardwareX-articles. 


Friday 09/02.24

Waiting for the CNC, we have moved our attention to writing.



Monday 12/02.24

Today, during the scrum session, it came forward that more time should be spent discovering different gripping mechanisms instead of only focusing on improving the existing gripping/clamping setup at MRCL. Therefore, we are going to use this week while we wait for the CNC to arrive on exploring clamping yet again.

Some molds for silicone clamping has been printed, and will be made ready tomorrow.


Tuesday 13/02.24

Today, silicone was poured into the clamping pin molds. They will be cured by tomorrow and be ready for small scale testing.

Also, Peter started on a design for a 6-clamp solution inside Fusion360. This design will be further improved once the CNC has arrived, and we know more about how we want to implement our clamping solution to the CNC.


Wednesday 14/02.24

Today, the silicone clamping pins were tested. How that went is described closer here. In addition, some more silicone clamping pins were made, with a harder silicone. 


Thursday 15/02.24

Today the CNC we had ordered arrived! We therefore have started planning on how to cut the frame so it fits inside the freezer.

In addition, the second iteration of the silicone clamping pins were tested. How that went is described here.

Friday 16/02.24



Monday 19/02.24

Today we finished measuring the x and y axes and cut them, along with their lead screws. They all fit nicely in the freezer.

We started by very precisely measuring the cutting-line. Then we brought the profiles and screws down to the workshop and got them cut.


The new profiles were prepared by filing down sharp edges and threading new M5x0.8 holes.


Finally the CNC axes were assembled by following the instructions.


Insert Images


Tomorrow we will finish the installation of the CNC while simultaneously thinking of how to install a stable z-axis and a well functioning clamping method. 

Tuesday 20/02.24

Today we started with improving the CNC.

We worked on the clamping mechanism


We also added a base board for extra stability and a more professional look. The plate is saved as BunnplateCNC.dxf.

The first iteration was made using 6mm MDF, to check if the measurements fit. Tomorrow, this will be made using 3 or 4 mm aluminium and a platecutter. 

To increase the stability and the friction against the freezer we mounted the legs that came with the CNC. They were mounted on top of the base plate using M5x25 screws. This would ensure stability, but would not collide with the wheels rolling through the profiles.


Wednesday 21/02.24

Today, the old MDF baseplate was replaced with a new baseplate in 5mm aluminium. In addition, the rear supporting beam was mounted to the CNC. The spindle motor was also mounted on the Z-axis setup, and work began planning where the Z-axis will be mounted to the CNC. 

Also, the clamping mechanism was also improved further. 


Thursday 22/02.24

Made the Z-axis support beam and pillars. Not mounted to the CNC yet. We explored what requirements our camera should have.


Friday 23/02.24

After some practical testing and some makeshift Lightburn calibration, we found that further camera-and-clamping work should not be conducted until the CNC is operational, as this will provide valuable insight.

The Z-axis has been mounted to the frame. It will be mounted to the CNC as soon as the T-slots and brackets from RS arrives.


Monday 26/02.24

Scrum with Martin and rest of Trolls today. Made support beams for the Z-axis frame. Continued development of the clamping prototype. Electronics were connected to the controller.


Tuesday 27/02.24

Mounted the Z-axis assembly to the CNC today. Also got vaccinated. Continued development of the clamping prototype.


Wednesday 28/02.24

Mounted the Z-axis assembly using the proper ordered t-slots and brackets. Found out that the support beams were an overkill as the brackets made the Z-axis assembly stable without the support beams mounted. Therefore, they are dropped from the CNC for now.


Thursday 29/02.24

We have begun discussing how high the clamping frame should be mounted and if some rollers should be included to reduce torque strain on the clamping attachment.


A camera mount is also in production.


Friday 01/03.24


Today we have continued development of the prototype. The clamping attachment finally fits right and we could get hands on experience with how the concept fits on the CNC bed.

We also go a visit from the MR Core labs team, which provided valuable feedback on the progress of the prototype and the vision going forward



Monday 04/03.24

Made a small 3D-printed version of some fractal vise clamps. Demonstrated them on the Scrum. 

Tuesday 05/03.24

Made a camera mount and a square clamping frame.

Wednesday 06/03.24

Øystein was sick today. 

Thursday 07/03.24

Peter was on winter holiday. Øystein made an arduino setup for 3 temperature sensors. 

Friday 08/03.24

Today, an attempt was made connecting the arduino directly to a CSV-file via python, but there was alot of problems with VSCode. Therefore, time was spent managing the cables for the CNC.


Monday 11/03.24

Made an iris closing mechanism to research pottential gripping methods. Will be pursuided further. Also started seting up Lightburn for the CNC and playing around with the software. Will make all the eletrical wires run out of the freezer so that we can close it and propperly begin testing by wednesday.

Tuesday 12/03.24


Today we made a temperature sensor array using an arduino uno with an ethernet shield and a SD-card. It will read the temperature from the 3 sensors and write it to file, so that it can be plotted by the python code on the SD-card afterwards.


Additionally, after some hassle, the CNC now communicated correctly with lightburn.

It was struggling with understanding the M4 commando (turning on the spindle), so we had to change the device board in the Lightburn settings.

 


Now the CNC functions as it should.




Wednesday 13/03.24

Made a new attachement plate with a cable slot for the camera to be mounted

Thursday 14/03.24

Today, the Lightburn programme was completed. In addition, the camera was mounted to the CNC. We found that a 90 degree USB-C adapter was needed to get a sufficient cable arrangement. This was therefore requested to be ordered. Lastly, we made a "pepperkake-form" of a prostate to easier be able to cut out ham slices more uniformly, and in the shape of a "prostate".


Friday 15/03.24


Today we prepped the ham for testing and upgraded our MDF base plate for an aluminum base plate.
We probably did more, but we forgot to write it down.


Monday 18/03.24

Today was master scrum and we got input on how the work was going and what to focus on going forward.
The message is clear. We should really test some more exiting clamping solutions. 

Therefore, going forward Peter will focus on the development of the CNC in the freezer, and Øystein will focus more on the innovation of clamping mechanisms. They don't have to be fully functional, but tested well enough for us to be able to provide some recommendations for future work. 

There is still no update from St.Olavs regarding the prostate cutting.


The day was spent making the final adjustments to the freezer (with regards to the door and the wires) for it to be ready for testing. 


Tuesday 19/03.24

We figured out what the issue with the CNC controller was. It turns out our controller is not a GRBL 1.1e or earlier, it is a MKS DLC32, that uses GRBL 1.1h, but there is something wrong with the current MKS DLC32 firmware that causes it to ot be able to interpret M4 (spindle on with variable speed) commands. We have found the resources that explain the issue and we have found the necessary firmware upgrade, but the firmware uploader for that board does not want to cooperate with my computer. In addition, we are afraid that if we upload new firmware, and something goes wrong, we wont be able to do testing until we get a replacement.

The resources can be found here:

https://github.com/makerbase-mks/MKS-DLC32/blob/main/MKS-DLC32-main/firmware/tool/CH340G_USB.zip

https://github.com/makerbase-mks/MKS-DLC32/blob/main/MKS-DLC32-main/firmware/readme.md

https://github.com/makerbase-mks/MKS-DLC32/blob/main/MKS-DLC32-main/doc/DLC32%20Firmware%20Programming%20Instructions.pdf

https://forum.lightburnsoftware.com/t/dlc32-m4-does-not-work/67127/6

https://forum.lightburnsoftware.com/t/mks-dlc32-device/99971/5


Further development of a possible iris clamping mechanism.


Wednesday 20/03.24

We decided to buy ourselves a GRBL. It is more familiar and it is smart to have a backup.
To work around the problem, we have made a python code that post-processes the g-code and makes it function the way we want it to function.


Preliminary testing was conducted and results can be found here


Thursday 21/03.24


Friday 22/03.24

We now have a working iris mechanism clamper who nicely forms around the MDF-prostate. The focus has now shifted towards securing the pins in place. First to be tested will be another cam-shaft mechanism.


Monday 25/03.24

Peter had a complete makeover of the cable system of the CNC. In addition, a  box with all the wires was added to the side of the freezer to make it look cleaner.

Tuesday 26/03.24

Worked on the tightner for the iris clamping mechanism.


Wednesday 27/03.24

Continued work on the clamping mechanism. Also installed light into the freezer, although this is not permanently mounted. Will need to find the best position for the LED-strip before mounting it permanently.

Also swapped from the chinese motherboard to the GRBL motherboard.

Thursday 27/03.24

Easter Holiday

Friday 29/03.24

Easter Holiday


Monday 01/04.24

Easter Holiday

Tuesday 02/04.24

Today was used to swap from the chinese circuit board to the GRBL. In addition, a new iteration for the camera calibration was made, as well as a new iteration to the attachement plate. The sensors were also installed properly into the freezer.

Wednesday 03/03.24

Mounted heatInserts into the new backplate to chech if it fits, which it did. The design is now ready to be sent to the waterjet to be made in aluminium. Also mounted the lights to the freezer with double sided tape. 

Thursday 04/04.24

Made the final design for the attachement plate and gripping plate. They wil be cut with the waterjet tomorrow. Started designing the final box for the electronics aswell.

Friday 05/04.24

Waterjetted the parts today


Monday 08/04.24

Scrum today. Made a hole in the bottom plate in preparation for the storage testing planned.

Tuesday 09/04.24

Today was cable organizing day. Mounted all the outside components to the outside of the freezer. The plan is to make a lid from some acryllic to mount to the side of the freezer to cover all the components.

On the inside of the freezer, the loose cables have been organized so that everything looks more nice. 

Wednesday 10/03.24

Made an improved design for the camera attachement. Also, made preparations for the test of the freezer. Started making the cover box for the outside of the freezer

Thursday 11/04.24


Friday 12/04.24


Monday 15/04.24

Started testing and making a collection system

Tuesday 16/04.24

Continued the work on the collection system. Continued testing.

Wednesday 17/03.24

completed the first iteration of the collection system. 

Thursday 18/04.24

Made a cover box for the electronics and a new version of the collection system. The last one was too unstable.

Friday 19/04.24


Monday 23/04.24

Scrum today. made a plan for the rest of the building process.

Tuesday 24/04.24

Collected the organs today and cut out samples. The liver slices was cut out from the centre of the liver. The tool used was a sharp big scalpel used for skin transplants.

Wednesday 25/03.24


Thursday 26/04.24


Friday 27/04.24

We are now done testing and very busy writing the thesis (heart) 

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